Monday, October 08, 2018
Fixing my lathe
While in operation in October 2017 the drive belt in my
lathe broke; it was shredded due to wear and tear. Alarm engulfed me. How was I
to find a replacement belt; getting the lathe itself was one long search.
Nobody sells such lathe in Singapore, and nobody sells one to Singapore, not
even the manufacturers in China. It was a hobbyist model, and there was no
woodturning hobbyist here yet. Finally I
got it in April 2014 after posting on the WWW. Harbor Freight in the US offered
a sale and delivered this Central Machinery lathe which like most lathes of
this kind were made in China.
The belt was tattered, no part number can be seen, so how
was I to tell people what belt I want. I carefully determined its dimensions,
width, thickness, cross section, number of ribs, teeth, circumference and type
of material. Hopefully with these details I could quote my belt as I could not
find any other detail on the broken belt. It occurred to me that it would be
futile looking for one in Singapore where no such machine has need of it. There
are belt shops around, but mostly they cater to the autocar industry. My
queries to people I know received no response. I was the only woodturner and
this problem was uniquely mine.
Amazon and Ebay were useless, they offered all kinds of
belt, but nothing near to what I needed. One road one belt was not around then,
ha ha. My best bet was Aliexpress, the home which manufactures billions of
things, and it was a China product I needed. Aha, myriads of belts were on
sale, but not one near to my requirements. Finally I found one with the same type
of ribs and cross groves, but it was not of the same width nor circumference. I
wrote to the seller, but I received no reply. But then a few days later, I
found a new posting by this same seller which offered one with the exact fit. Boy oh boy, overjoyed, I couldn’t care less
about the price, I placed the order on the spot.
I received the belt, and comparably all the dimensions fit,
the difference in colour did not matter. I had figured out exactly the
procedure I had to perform. All I needed was to loosen the handwheel, remove
the drive shaft and replace the belt and fix everything. But the drive shaft
was stuck fast, solidly stuck to the two ball bearings on each side of the
gears. The operation manuals were useless. So, the rescue operation was stalled
as it began.
Ha ha, good luck; someone on Youtube demonstrated how he
replaced the belt of his lathe of exactly the same model. Full of expectations I
followed his procedure, but the shaft held fast. Hammering harder and harder
did not work, and hammering too hard might break the bearings or crack the
housing. I had sounded like a blacksmith. So, the operation was stalled again.
I could take the whole unit to the car mechanic, but there was
no certainty of success. Worse still, the housing might become broken or the
bearings damaged, as the way car mechanics operate is well known. I had to be
prepared. I searched on the WWW again on the availability of the bearings. I
learned a full lesson on the types, functions, designs and usage of bearings
through my search, especially bearing interference. With this knowledge I finally
found the part number of the bearing on Aliexpress and that each cost a few
dollars. What a relief, the bearings will be available.
Somehow I went into chat sites on the WWW and got to know
about jaws and claws removers. These tools can remove bearings from shafts,
what luck. Again, my search went on, looking for claws with the right
dimensions. There were myriads of sites
selling two claws and three claws, but none were long and wide enough for my purpose,
they were mostly for straightforward removing of bearings from shafts, unlike
mine which is stuck in a housing. It was exasperating, with jaws and claws
everywhere but not a one that could fit mine. In desperation, I thought of
improvising, like removing the bracing struts to gain the full usage of the
length of the claws. So I placed my order for one, with the thought that should
that not work it still could be useful for other work which it might be
suitable.
The two claws were straight while the three claws were curve
but rearrange able for two claws operation by excluding one claw. The big
problem was that it was difficult to trust the general dimensions of the parts stated
in the postings. I wrote to several of the sellers and they all replied, but
they were useless without being as specific as what I had requested. However
one reply led me to figure out approximately from the pictures the maximum
capacity that it could handle. I immediately made the order.
The two removers arrived in good shape. The two claws did
fit with the bracings excluded, and I used clamps instead to hold the remover
in place. But as I screwed the spindle the pieces could not maintained their
hold and slipped apart, ha ha, proper job needs proper tools.
The three claws couldn’t embrace the shaft and bearing unit because
of the housing being too bulky. I adapted the remover to two claws and that
fitted. But then no matter how tight I screwed the spindle the shaft remained
intact, stuck fast to the bearings in the housing. However I was confident that
the operation was in the right direction, and one may not force things. So, I
left things hanging; and each day I tried to turn the spindle a little without
success.
Finally, I resolved to make or break. I took a bigger wrench
and used my body weight and applied with all my strength. Phiak … it was a very
short sharp sound. My thought was that the threads in the spindle had sheared
off, having read that in one of the chat sites. But the spindle was OK, and the
housing was not crack, and the two claws were OK too. Then I noticed that the
bearing had come out of the housing a few millimeters. Ha ha, it had worked,
what a relief. Finally with a few more tightening of the spindle the shaft came
loose with one bearing attached to it while the other bearing remained stuck in
the housing.
Well, with the dismantling work being done, the next step
was to clean everything and reassemble them. But when I tried to put the shaft
back it could not fit in, the outer ring of the bearing was bigger than the
bore of the housing, the difference was point two of a millimeter. This was
what I had learned about bearing interference, its design was calculated to
provide a tight fit to ensure that there would be no slippage. There was no way
I could use the three standard methods to force it in, by applying heat, by applying
cold or by using hydraulic force.
I used my rotary tool instead, and slowly and carefully
smoothened the inside of the bore. Well, one problem arose after the other, the
shaft also could not fit into the inner ring of the other bearing. Again, the
bearing interference was the same as with the other bearing. And again the
rotary tool was useful in smoothening the end of the shaft. So, after that I
did not expect any more problems.
And finally the belt was replaced and the lathe fixed, a
year later, October 2018.